Sunday, March 16, 2008
Coupling Issues Solved
I've replaced the X belt gear (hand-moulded perfectly first time) and strapped an old CPU fan onto the stepper. That takes care of cooling the X axis. Following that repair, I successfully printed a modified Y Motor Coupling and fitted it to the Darwin RepRap.
Using the new part, I then printed another identical coupling - so we know it lasts long enough to at least replicate itself. Note that the end away from the motor is somewhat thicker and there is a ridge running between the two grub screw holes. Here is one propped up by the working coupling on a pair of tweezers. Temperature graphs show motor temperatures halting below 45C, so the coupling issues seem solved.
The End?
Vik :v)
Using the new part, I then printed another identical coupling - so we know it lasts long enough to at least replicate itself. Note that the end away from the motor is somewhat thicker and there is a ridge running between the two grub screw holes. Here is one propped up by the working coupling on a pair of tweezers. Temperature graphs show motor temperatures halting below 45C, so the coupling issues seem solved.
The End?
Vik :v)
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Nice to see some examples of self-repair/self-organ-replacement going on. Seems like a natural step between the inert, inorganic collection of parts and a "living" reprap.
nophead: We need a fan anyway for cooling the workpiece. The stepper cooling fan should go away when we move to DC servos.
Vik :v)
Vik :v)
Yeah, where do you think mine came from :)
It'll be good to get rid of them eventually though.
Vik :v)
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It'll be good to get rid of them eventually though.
Vik :v)
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